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DSCF0272

DSCF0272

Date: 06/04/2004 Views: 4853

Fuel_System_10_001

Fuel_System_10_001

Date: 06/08/2007 Views: 4801

FillingFuselage20Ann

FillingFuselage20Ann

Date: 09/06/2004 Views: 3303

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EAA SITE

EAA SITE

Date: 08/23/2023 Views: 725158

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EAA SITE

EAA SITE

Date: 08/23/2023 Views: 725158

Most Viewed Items

Date: 12/21/2025
Owner: Guest
Size: 84 items
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IMG_3265

IMG_3265

Herein lies the culprit! The change from flat fiber washer to "O" ring. When the "O" ring is applied to the attachment screw and tightened to the torque spec, the bottom of the fuel bowl is deformed upward. This deformation reduces

Date: 05/30/2012
Views: 35524
IMG_0001post

IMG_0001post

Date: 07/12/2010
Views: 30584
IMG_1362ann

IMG_1362ann

2010 11 12 Was a total waste of a day. After arriving at the hanger, I went in to open the hanger door. When the hanger door had been opened I was greeted by the sight of a drooping rear bumper on the Ranger. Went to the droopy side and found this. R

Date: 11/12/2010
Views: 13958
IMG_3577post

IMG_3577post

Next test, connect high pressure port from airbox directly to the "T" into the carb float bowl pressure lines and try a run. Still didn't work. Same smooth up to 4200/4300 RPM, smooth drop to 3200 RPM, smooth acceleration up to 4300 RPM, drop

Date: 08/03/2012
Views: 11443
IMG_0017post

IMG_0017post

Date: 08/30/2010
Views: 9571
IMG_3438em

IMG_3438em

There was a bit more work with the Billet pump package, but it proved not to be the problem. Moving on, OK, not the fuel system. Try running the engine as a normally aspirated engine. Remove the connection between the turbo and airbox. Believe it or

Date: 07/17/2012
Views: 9426
IMG_3391em

IMG_3391em

Input fuel pressure: 5 lbs. Just like with the Billet pump. Next request was for a fuel flow test. Reconnected the Billet pump to the fuel circult. One electric pump running fuel through the billet pump produced 1 gallon of fuel in a bit less than 3 m

Date: 07/09/2012
Views: 9080
IMG_3540em

IMG_3540em

While the airbox was off, I again check all the pressure hoses to the carbs. Oh, what have we here. BIG leaks in the pressure lines to the carb bowls. Two leaks like this. Not observed before because the fittings were tied to that fuel line and the sp

Date: 07/30/2012
Views: 9032
IMG_3538em

IMG_3538em

I removed the entire airbox to to check all the plumbing connections.

Date: 07/30/2012
Views: 8610
IMG_3571em_r

IMG_3571em_r

Pulled all the pressure hose off again and check for leaks and continuity. All OK, no problems at all.

Date: 08/01/2012
Views: 8524
IMG_0241post

IMG_0241post

Date: 09/12/2010
Views: 8359
IMG_0013post

IMG_0013post

Date: 08/30/2010
Views: 8236
IMG_0003ann

IMG_0003ann

Date: 08/30/2010
Views: 8225
IMG_0002post

IMG_0002post

Date: 08/26/2010
Views: 8185
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IMG_0011post

IMG_0011post

Date: 08/30/2010
Views: 7918
IMG_0004post

IMG_0004post

Date: 08/30/2010
Views: 7848
IMG_2604

IMG_2604

Got out the inspection mirror and made sure the gasket was in place all the way round the bowl. It was.

Date: 05/30/2012
Views: 7633
IMG_3332em

IMG_3332em

Looks like that plug had been bumped some time during transport. Porcelain shows a crack. OK, replaced ALL the plugs. Engine still didn't run right.

Date: 06/12/2012
Views: 7560
New MC-4A 11

New MC-4A 11

Because the sides are narrower and closer to the ends of the MC-4A's the old outer spacers no longer fit and it would be impossible to further shorten them, they have been replaced with a couple washers.

Date: 04/15/2012
Views: 7355
IMG_0022post

IMG_0022post

Date: 08/30/2010
Views: 7266
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