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EuropaOwners N914XL - Bob Borger, N.Texas, USA: 99.0 hrs - Subsequent Flights Album has been updated as of 2016 05 16. Subsequent Flights
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N914XL - Bob Borger, N.Texas, USA: 99.0 hrs - Subsequent Flights Album has been updated as of 2016 05 16.

1. DSC_0064 2. First Flight 3. Subsequent ... 4. Tri-Gear... 5. Weight... 6. Aviation... 7. OSHKOSH 2007 ... 46. Fuel Tank...

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DSCN5776Ann

DSCN5776Ann

Date: 04/22/2007 Views: 5141

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24112003211025_G

Date: 12/31/1969 Views: 4219

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Scandinavia_662

Date: 06/13/2004 Views: 8529

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EAA SITE

EAA SITE

Date: 08/23/2023 Views: 857703

Subsequent Flights

I've been delinquent in my posts. I'll add some pictures of the aircraft as I have been flying it. And I'll add some pictures of North Texas from the last flights.

Date: 02/13/2009
Owner: rlborger
Size: 77 items (123 items total)
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We also put the graphics on his aircraft.

Date: 01/22/2010
Views: 4825
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Yup, that's Mighty Mouse. That was Gary's nick-name in the Navy. So it's fitting for the name of his Toot.

Date: 01/22/2010
Views: 4869
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We completed the metal installation as well as some radio wiring work and the graphics. I had hoped to work on my coolant leak today (23rd) but it's raining. Maybe tomorrow...

Date: 01/22/2010
Views: 4941
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2010 01 24 Went to the hanger to work on the coolant leak. Pulled the aircraft out, chocked it and tied the tail to the fence.

Date: 01/24/2010
Views: 4865
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Started the engine and let it run a bit and settle down. Started looking for signs of a leak. Took a bit, but finally found some coolant drops.

Date: 01/24/2010
Views: 4332
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First found them here.

Date: 01/24/2010
Views: 4862
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Then saw the drop on the engine mount cross-tube and saw more coming across the tube.

Date: 01/24/2010
Views: 5284
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Finally, back underneath to find the old drops on the cross tube and there was the tell-tale residue of evaporated coolant on the intake to the coolant pump (Green arrow). Shut things down. Found the longest screwdriver I had and was able to reach the c

Date: 01/24/2010
Views: 6031
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Put the aircraft back in the hanger and put the cowl back on to wait for a better day to fly.

Date: 01/24/2010
Views: 5915
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Because today it was a 30 degree X-wind gusting to 25 kts. Too much for me at this time. Maybe in another 10 - 15 hours... Might be good flying weather tomorrow after work. We'll see.

Date: 01/24/2010
Views: 4997
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