Login
EuropaOwners N914XL - Bob Borger, N.Texas, USA: 99.0 hrs - Subsequent Flights Album has been updated as of 2016 05 16. Subsequent Flights
Advanced Search
Mount with WebDAV RSS Feed for this Album View Latest Updates View Popular Items View Random Items View Slideshow (Fullscreen)

N914XL - Bob Borger, N.Texas, USA: 99.0 hrs - Subsequent Flights Album has been updated as of 2016 05 16.

1. DSC_0064 2. First Flight 3. Subsequent ... 4. Tri-Gear... 5. Weight... 6. Aviation... 7. OSHKOSH 2007 ... 46. Fuel Tank...

Random Images

IMG_1602

IMG_1602

Date: 04/13/2010 Views: 7031

Double header.

Double header.

Date: 10/24/2009 Views: 3261

Justin mono holder 2

Justin mono holder 2

Date: 01/06/2010 Views: 6504

Newest Image

EAA SITE

EAA SITE

Date: 08/23/2023 Views: 693561

Subsequent Flights

I've been delinquent in my posts. I'll add some pictures of the aircraft as I have been flying it. And I'll add some pictures of North Texas from the last flights.

Date: 02/13/2009
Owner: rlborger
Size: 77 items (123 items total)
nextlast
first previous
IMG_0858post

IMG_0858post

We also put the graphics on his aircraft.

Date: 01/22/2010
Views: 3998
IMG_0866post

IMG_0866post

Yup, that's Mighty Mouse. That was Gary's nick-name in the Navy. So it's fitting for the name of his Toot.

Date: 01/22/2010
Views: 3995
IMG_0868post

IMG_0868post

We completed the metal installation as well as some radio wiring work and the graphics. I had hoped to work on my coolant leak today (23rd) but it's raining. Maybe tomorrow...

Date: 01/22/2010
Views: 4074
IMG_0870post

IMG_0870post

2010 01 24 Went to the hanger to work on the coolant leak. Pulled the aircraft out, chocked it and tied the tail to the fence.

Date: 01/24/2010
Views: 4143
IMG_0869

IMG_0869

Started the engine and let it run a bit and settle down. Started looking for signs of a leak. Took a bit, but finally found some coolant drops.

Date: 01/24/2010
Views: 3607
IMG_0872post

IMG_0872post

First found them here.

Date: 01/24/2010
Views: 4002
IMG_0873post

IMG_0873post

Then saw the drop on the engine mount cross-tube and saw more coming across the tube.

Date: 01/24/2010
Views: 4523
IMG_0874post

IMG_0874post

Finally, back underneath to find the old drops on the cross tube and there was the tell-tale residue of evaporated coolant on the intake to the coolant pump (Green arrow). Shut things down. Found the longest screwdriver I had and was able to reach the c

Date: 01/24/2010
Views: 5036
IMG_0876post

IMG_0876post

Put the aircraft back in the hanger and put the cowl back on to wait for a better day to fly.

Date: 01/24/2010
Views: 4871
IMG_0877post

IMG_0877post

Because today it was a 30 degree X-wind gusting to 25 kts. Too much for me at this time. Maybe in another 10 - 15 hours... Might be good flying weather tomorrow after work. We'll see.

Date: 01/24/2010
Views: 4236
nextlast
first previous
Page: 1 2 3 4 5 6 7 8
Powered by Gallery v2.3